Showing posts with label repair. Show all posts
Showing posts with label repair. Show all posts

Thursday 14 January 2016

Plastic repair!

There are only so many jobs that you can do for yourself when it comes to working on your van. I, like the rest of you, have to use other service providers for certain jobs. The main one being tyres, it is far better to let them do the job - seeing as they have all the kit!

OK! with that in mind we had a couple of tyres that needed to be replaced because they had worn out. So, took the van in to get them replaced.

A couple of days later I noticed something was flapping about under the van, which was strange, so I decided to have a look, jacked the front up and discovered what looked like a mud flap/ deflector at the back of the wheel arch which was not broken before the new tyres were fitted. I do not like complaining or pointing the finger at other trade professionals because I have been on the end of “It was OK until you worked on it” situation. In this case however I'm going to complain. Why? Because they had also drilled the wheel nuts on so tightly, I had to use a meter long handle on my breaker bar with socket to move it! They should know better! They don't know it, but we now use another tyre fitter for all our work.

 The upside of this is that our good friends at Plasweld were able to weld the broken plastic back together. Which saved us having to track down an expensive replacement. They are wizards with anything plastic whether motor related or not.

To show our appreciation I'm going to point you in their direction of Plasweld - I know the web site shows a lot of motor bike work but do not let that put you off. The same materials are used by both car and bike etc.


Sunday 19 October 2014

Replacing track ends. the pit falls.

the track rod ends on these vehicles are handed
nearside and offside.
Track rod end or track control arm ball joints no matter what you call it, it's at the end of the steering rack arms. For such a small ball joint it takes a lot of abuse from us the driver hitting curbs, bumping up them to park and potholes. It is surprising that they do not fail more often. It is all these little knocks and bump over time that led to them failing before they should. In most cases they are not noticed until they fail the MOT, or the worst-case scenario give up the ghost while we are driving down the road. I have been witnessing to number of these over the years.

There are some tell tail signs to alert us to their wearing out. Most of them do not happen until they are quite loose in the ball joint knuckle. Adverse wear on a tyre is one indicator. This looks like a tracking problem; what sets it apart from tracking is that the tyre looks more worn one side than the other. Another is an occasional slight wobble on the steering when gently braking. Unless you are very tuned in with your vehicle you will not notice it.

Once the bad news is in that your transport failed the MOT it is not that difficult a job to do. But I know there are a couple of 'buts' to take into account, even so, they do not add that much drama to the job.

Once the wheel nuts are loosened jack the vehicle up and place an axle stand under to support it just in case the jack fails. It does happen. Take the wheel off and turn the steering so the steering arm is fully extended this will allow fuller access to the ball joint. The first thing to do is loosen the tack rod end locking nut on the steering arm. These can be difficult to loosen, it is a good idea to soak it in freeing oil. You will have to use a C spanner on this nut so be careful as these spanners have a nasty habit of slipping off. 

Shocking ball joint loose

Now-a-days most ball joints are held in place with a Ni-lock nut the thread above the nut is most likely badly rusted. This is where an impact wrench is handy as this bit of kit will have the nut undone in no time. Again, soak in freeing oil. What happens is the nylon of the nut locks solid on the rusty thread which then brakes the taper hold allowing the whole thing to spin in place. Now the fun begins. If this happens you will need the jack to push the ball joint back into place. This will mean that you almost lift the van off the axle stand to recreate the hold it had. This is one of the only ways of doing it. Now you need a blow torch or nut heater so the nylon can be melted, and the nut expanded. While it is red hot it is possible to put a socket on it to complete the nuts removal. You will need to work quickly as the heat dissipates from the nylon allowing it to reform locking the nut again. Alternatively, you can if you have one use a nut splitter.

If the nut comes off as it should the ball joint now needs to be separated from the hub arm. There are a couple of ways of doing this, use a ball joint separation tool or jar it lose with a heavy hammer, this method is not for the faint heated.  It is my favoured way but then I have had a lot of practice honing it down to a fine art. If you decide to go this route, I suggest binding the handle where it meets the head of the hammer with plastic tape the type electricians use. You will need to wrap it around quite a few times. The reasoning behind this is if you miss, which you will, the hub arm will strike the hammers handle, the tape stops bits being taken out of the handle lessening the chances of the head being broken off. You will need to hit the arm with some force to get it to loosen and in most cases several hits will be required to get it to shift.

Please note: do not use the method described above unless you are confident to do so. Getting it wrong may damage the van and yourself. You have been warned.

wheel nut rotation of tightening
Once off, it is a good idea to count the number of turns it takes to remove the track rod end from the steering rack.

With the new track rod end in hand thread, it on to the arm the number of turns it took to take it off. By doing this it should return the tracking to what it was before you removed the old one. Lessening the need to get the tracking adjusted straight away.

Put the ball joint thread through the hub arm and tighten the nut to (37). Re tighten the steering rack nut to the back of the ball joint, it is a good idea to put a bit of copper grease on the thread to make it easier to undo next time. Put the wheel on, thread the bolts on and nip tight, drop the jack and tighten the wheel nut up to (140) in a diagonal rotation. This makes sure that each bolt is evenly tightened.

Please note that the numbers in the brackets (00) are torque wrench settings in Newton meters.

Friday 30 November 2012

The smell of burning!


Overheated rear brake disc.
I was in a hurry the other day to get the dog to the vet. It was not until I was part way up the bypass that I realised that the handbrake had stuck on. Even though the hand brake leaver in the cab was completely off, the smell of brake linings was overpowering. It's just as well the vets was not too far, even so the back wheels were so hot you could not touch them. Just before we made the return journey I slipped under the van and pulled back the little arms that operate the handbrake on the back of the callipers. Man, they we tight! This does not bode well for those new wheel bearings that were fitted earlier in the year. A sticking hand brake is one of the reasons why the bearing failed in the first place!
 

Showing handbrake arm on Calliper
With the back of the van up in the air and both the wheels off, it is time to get to grips with sorting this problem out. On further investigation it turns out that the shaft that sticks out of the back of the calliper with the handbrake actuation arm on, has rusted tight. Even though there is a little rubber cup that sits between the calliper and the arm to protect the shaft from the weather. I believe this is its downfall because once the water gets behind the seal it remains there helping the rust to build up causing it to seize. 

 
Once the handbrake cable has been loosened you can remove the end of the cable from the arm more easily, with a bit of fiddling. To free the arm off you will need to tap it backwards and forwards with a medium weight hammer. Do not over do the amount of force you use when hitting the arm with the hammer. The idea is not to do it in one hit but to keep moving it up and down until the sprung loaded arm moves back to the off position on its own. When it feels like it has freed off enough to move it easily by hand, you need to check it's at the off position. If not, it is time to take a closer look at the spring. If the metal of the spring is pitted and heavily rusted it is possible that it has lost some of its tension. For the three or so pounds each it costs to replace these springs it is not worth messing about. Removing the spring from the arm is a bit annoying but straight forward with a pair of pliers.

Handbrake arm spring old and new

 
There is one last thing to do as a suggestion before you box it up and that is to get some white grease and push it in behind the little rubber seal that protects the handbrake arm shaft this will help to keep things moving and the weather out.

 
I have used this method on my van and so far, the hand brake has not stuck on again.


 
Related post   rear wheel bearing replacement.
 

 

 


Tuesday 4 September 2012

Vivaro couldn't pull the skin off a rice pudding.


The van has developed a running fault that started a month or so ago and has become progressively worse. It has taken us some time to chase down the cause of this problem.


The symptoms:

 This fault shows it's self when you drive away from a stand still. You have to push down the accelerator pedal a lot further than is normal to get it to speed up enough to change up to second gear. On lifting your foot off the accelerator pedal to change gear the vehicle speeds up while you are changing up. On pressing down on the pedal again the van struggles to gain speed. It feels like it is holding back.

 
Thought process and action.
 
This suggests that it is a fuel problem. But it has nothing to do with fuel, injectors, high pressure pump, fuel filter or related sensors. Another suggestion was the turbo, but we could hear it spooling up. We checked the turbo pipes, ducting was tight and not blocked. We found a couple of lose hose clips but not enough to cause power loss. Also checked to make sure the waste gate solenoid worked as it should.

At one point we thought the ECU needed a re-boot, again it did not seem likely. Thinking about it, it was a flow problem the only other thing that came to mind was the air flow meter. Before we paid out on a new meter we surfed some motoring forums for pointers, but no one had this fault it would seem. We came across a thread that suggested the changing of the airflow meter would sort it out, but this gentleman also had the crank sensor replace. After a short discussion we decided to go with the air flow meter. Bingo! got it in one and what a relief, it would have been an expensive mistake otherwise.


Air flow meter
 

Extra work.

 
While we had the air filter housing off, which is a pig remove, we thought it prudent to check the glow plugs as it only takes a couple of minutes with a voltmeter. We found that two of the plugs didn't work. The ERG valve drew my attention because the inlet manifold was covered in oil suggesting the gasket had failed or the bolts were loose. You have to be patient when removing it as it has a build-up of oil residue. On removal, it was found clogged with a thick coagulated oil that took a bit of cleaning up.
 

It runs and pulls like a train now. The rice pudding skin doesn't stand a chance!